Difference between revisions of "Novena EVT to DVT changes"

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| R21A 100, 1% | R21A 20 ohms, 1%,0402 || 10 ohm on EVT1A, but should be effective at 20 ohms. 10 ohms would be a new component, if lower value is needed go to 8.06 1% (from R10N)
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| R21A 100, 1% || R21A 20 ohms, 1%,0402 || 10 ohm on EVT1A, but should be effective at 20 ohms. 10 ohms would be a new component, if lower value is needed go to 8.06 1% (from R10N)
 
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Revision as of 10:37, 19 March 2013

Novena EVT to DVT changes

This is a list of all the changes applied to the board from EVT1A to DVT1 release. If it's not on this list, it didn't happen.

Each change has the format of issue summary/resolution, and specific change

ECO1: Inrush current limit

The RC constant governing the turn-on/turn-off rates of the FET power switches needs tuning. In EVT, most switches are turning on too quickly for them to be effective. Resolution is to increase capacitance and resistance.

EVT DVT Notes
R38N 330, 1% / REC1005N R38N 10k, 1% / RESC1005N P3.3V_DELAYED
C30N 0.1uF, 6.3V, X5R / CAPC0603N_B C30N 1.0uF, 25V, 20% X5R 0201 / CAPC0603N_B P3.3V_DELAYED
R29N 330, 1% / REC1005N R29N 10k, 1% / RESC1005N P5.0V_DELAYED
C27N 0.1uF, 6.3V, X5R / CAPC0603N_B C27N 1.0uF, 25V, 20% X5R 0201 / CAPC0603N_B P5.0V_DELAYED
R11H 330, 1% / REC1005N R11H 10k, 1% / RESC1005N SATA_PWRON
C10H 0.1uF, 6.3V, X5R / CAPC0603N_B C10H 1.0uF, 25V, 20% X5R 0201 / CAPC0603N_B SATA_PWRON
C10X 0.1uF, 6.3V, X5R / CAPC0603N_B C10X 1.0uF, 25V, 20% X5R 0201 / CAPC0603N_B PCIE_PWRON
R15L 1k, 1% / REC1005N R15L 10k, 1% / RESC1005N LCD_VCC_SW
C14L 0.1uF, 6.3V, X5R / CAPC0603N_B C14L 1.0uF, 25V, 20% X5R 0201 / CAPC0603N_B LCD_VCC_SW
C19L 0.1uF, 25V, X5R / CAPC1005N C19L 1.0uF, 25V, 20% X5R 0201 / CAPC0603N_B LCD_BL_VDD

ECO2: FPGA boot fuse interference

FPGA's internal pull-ups on boot will yank boot fuses to the CPU, causing wrong boot source to be selected.

EVT DVT Notes
R12F 4.7k, 1% / REC1005N R12F 4.7k, 1% (DNP) / RESC1005N depop pull-down
R13F 4.7k, 1% (DNP) / REC1005N R13F 4.7k, 1% / RESC1005N populate pull-up

ECO3: Gbit Ethernet Reset

Default circuit recommended by reference design is bogus. Get rid of it.

EVT DVT Notes
C32G 10uF, 10V, X5R, 20% removed
D11G BAT54T1G removed
D12G BAT54T1G removed
R20G 10k, 1% R20G 10k, 1% (DNP) also changed to pull to ground by default

ECO4: PCIe power on

Wire PCI express power on line (gate of Q10X) to ball R1 / pad name GPIO_17 / "GPIO7[12] aka 6 * 32 + 12 = GPIO 204". Software change required

ECO5: Improve magnetics termination

The magnetics in the PHY are not terminated properly, causing ISSI.

EVT DVT Notes
R14G 0 ohm R14G 0 ohm (DNP) also move EN1G_3.3VA line to other side of decaps on CT

ECO6: Gbit reflcock SI

Drive strength of U10G is not strong enough to overcome series terminator. Replace with shunt.

EVT DVT Notes
R21G 49.9, 1% RESC1005N R21G 0 ohm RESC1005N Double-check routing, consider RC shunt terminator

ECO7: HDMI HPD polarity

HDMI HPD polarity is not software programmable, so need to buffer (not invert) incoming signal.

EVT DVT Notes
R28L 0 ohm R28L 0 ohm (DNP)
R27L 0 ohm (DNP) R27L 0 ohm
Q17L 2N7002W (DNP) Q17L 2N7002W
R29L 10k, 1% (DNP) R29L 10k, 1%

ECO8: Audio chip sucks (power)

During power down, audio chip totally leaks power through the I2C bus. Need to really strengthen the pull-down to fully reset the chip and fight the pull-ups on I2C.

EVT DVT Notes
R21A 100, 1% R21A 20 ohms, 1%,0402 10 ohm on EVT1A, but should be effective at 20 ohms. 10 ohms would be a new component, if lower value is needed go to 8.06 1% (from R10N)


  • APX803-44SAG-7 added, monitoring the P5.0V line, and pulling down the RESETBMCU line.
  • add 2.2k resistor in shunt with input capacitor network (BATT_PWR to ground)
  • Cut ALRCK trace to U11A, and jumper pin 9 of U11A to LCD_BL_ON
  • Rewire LCD_BL_ON to a new GPIO on the i.MX6 (final GPIO TBD)
  • Connect PICE_PWRON to i.MX6 (final GPIO TBD)
  • DDC_SCL changed to driver-only to prevent DoS attack on device via HDMI port