Difference between revisions of "Novena AFE"
(→EVT bringup notes) |
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*R17P is wrong. The current value of 45k sets the output to 3.3V. Should be 52.3k to set the output to 3.7V | *R17P is wrong. The current value of 45k sets the output to 3.3V. Should be 52.3k to set the output to 3.7V | ||
*R21C, R20C is too weak. Set to 1k to overcome the internal bias on SP0,1 | *R21C, R20C is too weak. Set to 1k to overcome the internal bias on SP0,1 | ||
+ | *Capacitive loading of VCMO is too large for 0-ohm stability with buffers. Replace R10I, R11I with 620 ohm, 1% resistors. Some tuning could be used later on, e.g. values were chosen conservatively large for stability, but if ripple appears on the line consider reducing resistor to improve ripple performance. | ||
+ | |||
===Loop filter tuning=== | ===Loop filter tuning=== | ||
Generated using ADIsimCLK - save file ad9520-3-calck.clk | Generated using ADIsimCLK - save file ad9520-3-calck.clk | ||
Line 31: | Line 33: | ||
Delay from Ref to OUT3 is 250ps | Delay from Ref to OUT3 is 250ps | ||
</pre> | </pre> | ||
− | |||
==DAC-specific== | ==DAC-specific== | ||
U14A footprint is flipped. Must rework before power-up. | U14A footprint is flipped. Must rework before power-up. |
Revision as of 10:07, 10 March 2014
Notes on Novena AFE
EVT bringup notes
- R17P is wrong. The current value of 45k sets the output to 3.3V. Should be 52.3k to set the output to 3.7V
- R21C, R20C is too weak. Set to 1k to overcome the internal bias on SP0,1
- Capacitive loading of VCMO is too large for 0-ohm stability with buffers. Replace R10I, R11I with 620 ohm, 1% resistors. Some tuning could be used later on, e.g. values were chosen conservatively large for stability, but if ripple appears on the line consider reducing resistor to improve ripple performance.
Loop filter tuning
Generated using ADIsimCLK - save file ad9520-3-calck.clk
- C38C 1500pF -> 82pF
- R23C 3k -> 2.7k
- C37C 4.7uF -> 3.3nF
- R25C 2.1k -> 1.3k
- C36C 2200pF -> 270pF
- Loop bandwidth: 102 kHz
- Phase margin: 43.6 deg
- Zero: 37.1 kHz
- Pole: 275 kHz
- Last pole: 951kHz
Estimated phase noise and jitter to ADC:
Frequency: 1.00000GHz Broadband Jitter (>1kHz) = 558fs rms SNR = 69.10dB ENOB = 11.52bits at IF Freq = 100MHz Integrated Phase Noise from 100kHz to 1.25MHz Timing Jitter = 302fs rms Phase Jitter EVM = 0.19 %rms Phase Jitter = 0.109 degrees rms ACI / ACR = -57.5dBc Delay from Ref to OUT3 is 250ps
DAC-specific
U14A footprint is flipped. Must rework before power-up.